[NASSP 8][Apollo 9] Realtime simulation Debriefing

STS

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Hello all,
It´s again time for another Real Time Simulation debrief, this time for Apollo 9, wich we started on January 7th and concluded on January 17th. I continue to do these debriefs as I think that they provide usable feedback for NASSP´s users and the dev team.
For Apollo 9 I considered the flight days as follows:
  • FD1 (07/01/2023) GET -04:45:00 to GET 10:45:00
  • FD2 (08/01/2023) GET 19:00:00 to GET 30:00:00
  • FD3 (09/01/2023) GET 39:00:00 to GET 58:30:00
  • FD4 (10/01/2023) GET 66:30:00 to GET 79:00:00
  • FD5 (11/01/2023) GET 86:30:00 to GET 105:00:00
  • FD6 (12/01/2023) GET 112:30:00 to GET 130:00:00
  • FD7 (13/01/2023) GET 138:30:00 to GET 154:00:00
  • FD8 (14/01/2023) GET 162:00:00 to GET 177:00:00
  • FD9 (15/01/2023) GET 184:20:00 to GET 201:00:00
  • FD10 (16/01/2023) GET 207:40:00 to GET 223:00:00
  • FD11 (17/01/2023) GET 232:00:00 to [EOM]
For this Apollo 9 flight I used a joystick and a wireless numerical keyboard as an improvised THC/TTCA. I was able to place this improvised THC/TTCA vertically on my left hand.

Flight day 1:
For the first day of the flight of Apollo 9, the following activitied were to be performed:
  1. Startup checklist and backup crew prelaunch procedure
  2. Prime crew prelaunch procedure
  3. Saturn V Boost procedure
  4. Post insertion checks and config
  5. Pre CSM/LV sep, transposition and docking checks
  6. CSM/LV sep and transposition and docking
  7. Tunnel pressure verification & equalization
  8. LM ejection
  9. First S-IVB restart observation
  10. SPS-1 burn
  11. Daylight star check
  12. G&N power down
Startup checklist and backup crew prelaunch procedure:
Procedures were started at L -3:59:13, and this time I used the Checklist MFD. I took a pitstop to the bathroom between L -3:11:00 and L -03:01:00, as I waited for the next procedure to start at L -03:00:00. Procedures were complete at L -02:56:10.

Prime crew prelaunch procedure:
Crew ingress started at L -02:39:55 and the hatch was closed by using the clickspot on the VC at L -01:39:32.

Saturn V Boost procedure:
The fourth Saturn V to fly lifted off at 11:00:00 local time. Cabin pressure decrease was observed at GET 71 seconds, "Slowly but going". Suit temperature was high already (85ºF around GET 73 seconds, not noted yet by crew). SIC inboard engine shutdown occured at GET 2 minutes 15 seconds. SIC staging occured at GET 2 minutes and 47 seconds. SII engines ignition occured at 2 minutes and 49 seconds. Tower jett was done at 3 minutes 19 seconds. Suit temperature was 88ºF at GET 3 minutes and 41 seconds. Suit temp was started to be observed by crew at GET 4 minutes. Still GO at GET 5 minutes. And 6 minutes. Suit temp was 90ºF at 6 minutes 25 seconds. GO at 7 minutes. PU shift occured at GET 00:07:32. GO at 8 minutes, crew reported concerned about the suit temp at 8 minutes, as never noted that on trainings. 90ºF at 8 minutes. GO at 9 minutes. SII staging ocurred at 00:09:07 GET. S-IVB ignition occured at 00:09:11 GET. Go at 10 minutes, MCC said "No action" on suit temperature. SECO ocurred at 00:11:22 GET. Insertion data was as follows:
N44 HA +01050
N44 HP +00985
N44 TFF -59 59
N62 VI +25554
N62 H DOT +00015
N62 H PAD +01041

Post insertion checks and config:
Steps for post-insertion were started at 00:12:45 GET. Checklist MFD was also used for these procedures. MCC came up with troubleshooting for Suit high temp at around 00:17:25 GET. GLYCOL EVAP TEMP OUT was above 50.5ºF. Suit temperature was observed decreasing at 00:19:35 GET, after doffing helmet and gloves and changing the ECS config. Said temperature stabilized at around GET 00:30:00, at 75ºF.
@GET 00:36:00
H2 QTY %: 97
O2 QTY %: 97
@GET 00:38:00
FC1: 19.7A
FC2: 24A
FC3: 16A
MNA: 28.5V
MNB: 29V
SCS ATT Comparison check:
DSKY (IMU): +18000 +02678 +00145
ATT Set dials (IMU): 180 27 1.4
-------------
DSKY (GDC): +17984 +01667 +00137
ATT Set dials (GDC): 180 17 1.4
SPS Monitoring check:
@GET 001:31:50
Oxid QTY: 88.5%
Fuel QTY: 88.5%
Unbalance: 0
Rest of meters, OK
Optics dust cover jett was performed at GET 00:42:30.
Transcription of launch debrief performed by crew at 01:07:30:
"I think It was a nice launch, everything pretty nominal. Could see the yaw maneuver, and then the roll maneuver and the pitch maneuver went... went good, Uhm... Staging went... went OK from the SIC uhmmm... went on time. No problems there. And then during Stage 2 we saw that the suit temperature was high, or... that was... what at least it seemed like, it was around 95 degrees, pretty high, didn´t saw that on the simulations ahh... concerned a lot, a bit but continued uhhh... and on orbit when we were preparing the ECS for orbit stay the temperature normalized so we are okay there. So yeah, the launch went smooth, the S-IVB ignition... scared us a little bit because when you are doing this for real the time that the engine one light stays out scares you, scares you a little bit. But it was everythiong pretty nominal. Ahh. We had an apogee of 105 miles and a perigee, ahhh..., of 98.5 miles, an insertion velocity of 25554 feets per second at an altitude of 104.1 miles. And that was our launch."
Post insertion checklist was completed at 001:34:50 GET.

Pre CSM/LV sep, transposition and docking checks:
Stayed on Checklist MFD (on the previous missions, as I used the good old Word checklists now it would be the time to go to Checklist MFD)Docking probe extension occured at 01:50:15 GET. Nominal extension, two gray talkbacks. Primary Glycol Evaporator was disabled at GET 002:00:00.
Cabin purge was also terminated there. Cabin pressure was increased to 5.7 PSIA. Auto RCS switches were all set to MNB as per checklist. Crew saw two V46´s around 002:29:00 GET and was confused about that. MCC said no issue there, and crew did them. SM RCS was tested at 002:25:26 GET.

CSM/LV sep, transposition and docking:
Pyro arm for separation was performed at 002:45:09 GET. Before separation crew asked if the pitch error needle was all right. Crew was nervous and human factors related things started to kick in. Crew set the event timer to +20 seconds, to have time to synchronize with a timer I had on hand and that I would activate at the same time that I pressed the "6" key on my improvised THC. Separation ocurred on time at 002:47:02 GET but crew forgot to put EMS mode to normal. Pitch rate for pitcharound was 1.5º per second and it was started at T+38 seconds. EMS was corrected to -100.8 at T+75 seconds, but it was not clear if we were moving away from S-IVB at the planned speed of 0.8 fps. DSKY showed +00006 -00001 +00005 at T+80 seconds.
S-IVB was observed thru side hatch at 002:49:25 GET, T+ 2:26, DSKY showing -00006 -00001 +00006. SLA panels were seen jettison correctly and docking target was clear, Spider seemed to be sleeping peacefully on her nest.
Keepstation was started at T+3 minutes. Due to the EMS mistake earlier, it was harder to determine if closing in to the LM or drifting away from it during keepstation.
Approach to LM was started at T+14:14, with the GDC align 30 seconds earlier. 1 fps was the initial closure rate, applied to +X. During approach the S-IVB and LM were never outside the COAS indicator. Final approach and soft docking speed was a little bit fast. Attitude was very well aligned before capture. Translation was a little bit off to the right before capture.
Capture occured at GET 003:07:22, T+20:23. Retract commanded at T+20:48, hard dock occured at T+20:51.
State vector update and NAV CHECK PAD were received at GET 003:15:00. Nav check PAD was:
NAV CHECK
N34 HRS +00033
MIN +00045
SEC +00001
N34 LAT -02795
LON +04062
ALT +01004
P21 agreed with NAV CHECK PAD after the state vector update.

Tunnel pressure verification & equalization:
At GET 003:25:15, surge tank pressure was checked and was at around 895 PSI. At GET 003:25:57, air was started to be introduced to the LM, thus equalizing the pressure between the CM and the LM. At GET 003:28:25 Delta pressure between CM and LM was 3.1 PSI. No leaks were detected. At GET 003:31:25 pressure equalization valve was opened again. CM Repress O2 valve was opened for the first time at GET 003:33:33, and closed at 003:34:05. Second cycle of repress was between GET 003:42:20 and GET 003:43:39. Procedure was complete at GET 003:45:35. Surge tank pressure was "refilled" as last step of the procedure.

LM Power to CSM was activated at GET 003:46:42.

LM ejection:
Cabin purge was resumed at GET 003:58:10. DAP was reconfigured for CSM/LM flight and pyros were armed at GET 004:00:10. LM separation from LV occured at GET 004:08:00, and a -0.5fps was gained on the +X axis. Auto maneuver to evasive maneuver attitude was started at T+35 seconds. Evasive maneuver was performed at T +02:58, and a -0.5 fps was applied to the +X axis, firing -X for 3 seconds.
Visual contact with S-IVB was maintained without issue. At GET 004:14:00 crew estimated distance to be 70 feet. As expected, a little bit of pitch rate was required, and also a monitoring of attitude to not enter gimbal lock.

First S-IVB restart observation:
S-IVB attitude change to RPY 0,0,0 was noticeable at GET 004:26:00. S-IVB Restart was observed at GET 004:45:28 GET.

SPS-1 burn:
PAD for SPS-1 burn, wich was intended to change to a 128*113 orbit was received at GET 004:50:00. Was as follows:
MANEUVER UPDATE (P30)
SPS-1 PURPOSE
+00005 HR TIG N33
+00059 MIN
+000.00 SEC
+0036.8 DVX LOCAL VERT N81
+00000 DVY
+00000 DVZ
+0036.8 DVR N42
+0032.4 DVC
0:05.0 BT
+58867 CSM WT N47
+001.05 PTRM N48
-000.23 YTRM
15 SXTS
26.59 SFT
10.633 TRUN
+000.00 LAT NAV CHECK
+000.00 LON
+000.00 ALT
000 R
356 P
001 Y
Remarks: Gimbal angles with PAD REFSMMAT
SPS-1 burn prediction was obtained at GET 004:52:23 and was:
HA +0125.1
HP +0102.8
DVR +0036.8
Spacecraft control mode was set to FREE around GET 005:15:00 for the P52 option 3 realign. At GET 005:18:15 DAP config was verified with MCC, it was 21111 11111 on N46.
Alignment check was started at GET 005:21:20, and completed at . Crew did a mistake at GET 005:24:30, by changing again CMC mode to FREE and maneuvering to a different attitude. What I wanted to do was to select another couple of stars. That caused the held burn attitude to be lost. MCC reported the problem, as crew didn´t notice it at all. P40 wanted to burn at RPY +304.86, +356.54, +000.97, because it was the attitude the spacecraft was at when calling P40. Also, P40 was called from P00, causing that, by following the checklist too correctly, an F50 25 with code 00204 was shown early, when I was to move the optics to the star check angles. Solution given was go back to P00, and V49 again to the burn attitude. Auto maneuver to burn attitude was reperformed at GET 005:40:00. After auto maneuver was complete, P40 was started again at GET 005:42:00, now with a more adequate attitude and then continued the checklist with star check, but star check failed as I was 13 minutes behind and V41 N91 was entered at the F50 25 again. As of that, another P40 reselection was done at GET 005:47:17.
Burn was performed using SPS at GET 005:59:00. Burn duration was 5.some seconds. Both banks were used. Residuals as follows:
+00004
+00003
-00000
EMS Counter: -4.1
Not nulled as per mission rules.
Post SPS-1 orbit was:
HA +0124.3
HP +0102.9
SPS Oxid and fuel were 87.7% and no unballance after SPS-1. No ullage was used. SPS-1 was declared a good burn.
Daylight star check:
Star check PAD was as follows, received at 06:15:00 GET:
STAR CHECK UPDATE
006 HR GET
49 MIN
045.00 SEC
+068.0 R FDAI
+291.1 P
+330.2 Y
Most visible star was 23 (Denebola), at Sunrise, Sunrise + 5 minutes and Sunrise + 10 minutes.

G&N power down:
At GET 008:55:00 G&N was powered down for the first proper sleep cycle of the Apollo program.
Crew started an sleep cycle between GET 010:25:00 to GET 018:10:00.
 

STS

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Flight day 2:
After completing the first "proper" sleep period of the Apollo program, flight day 2 started. The following activities were to be performed:
  1. G&N power up
  2. SPS-2 burn
  3. SPS-3 burn
  4. SPS-4 burn
  5. G&N power down
G&N power up:
Procedures for G&N power up started at GET 18:50:00, with a CMC power up without issue at 18:50:25. Rest of procedures were complete, including a P51 IMU orientation at GET 19:52:47.

SPS-2 burn:
PAD for SPS-2 burn, wich was intended to change to a 192*113 orbit was received at GET 020:37:00. Was as follows:
MANEUVER UPDATE (P30)
SPS-2 PURPOSE
+00022 HR TIG N33
+00009 MIN
+002.48 SEC
+0099.1 DVX LOCAL VERT N81
-0851.3 DVY
-0000.2 DVZ
+0857.0 DVR N42
+0852.1 DVC
1:52.6 BT
+58504 CSM WT N47
+001.50 PTRM N48
-000.23 YTRM
21 SXTS
208.78 SFT
14.529 TRUN
-029.22 LAT NAV CHECK
-170.37 LON
+0117.5 ALT
000 R
000 P
000 Y
Remarks: None
Click to expand...
An state vector was uplinked from MCC, and P21 agreed with the NAV Check portion of the SPS-2 maneuver PAD.
SPS-2 burn prediction was obtained at GET 020:45:27 and was:
HA +0190.0
HP +0102.8
DVR +0857.0
An alignment check was performed prior to the burn, starting at GET 021:23:50. 4 stars were used, 4 and 6, and 42 and 34. Alignment check passed.
Burn was performed using SPS at GET 22:09:02. 40% stroking was applied at T+66 seconds. It was observed that DAP was slow to correct yaw and pitch error. Burn duration was 1 minute and 52 seconds. Both banks were used. Residuals as follows. Crew nulled Y residuals by mistake:
+00000
+00000
+00002
EMS Counter: -5
Not nulled as per mission rules.
Post SPS-2 orbit was:
HA +0188.1
HP +0102.8
SPS Oxid and fuel were 69.6% and no unballance after SPS-2. No ullage was used. SPS-2 was declared a good burn.

SPS-3 burn:
PAD for SPS-3 burn, wich was intended to change to a 270*115 orbit was received at GET 023:55:00. Was as follows:
MANEUVER UPDATE (P30)
SPS-3 PURPOSE
+00025 HR TIG N33
+00014 MIN
+047.14 SEC
+0015.3 DVX LOCAL VERT N81
-2549.6 DVY
-0000.1 DVZ
+2549.6 DVR N42
+2543.2 DVC
4:43.8 BT
+51136 CSM WT N47
+001.28 PTRM N48
-000.29 YTRM
22 SXTS
046.01 SFT
16.143 TRUN
+021.00 LAT NAV CHECK
+170.46 LON
+0151.4 ALT
000 R
000 P
000 Y
Remarks: None
Click to expand...
An state vector was uplinked from MCC, and P21 agreed with the NAV Check portion of the SPS-3 maneuver PAD. P21 had to be run twice as on first run crew did a mistake that consisted on pressing PRO before ENTR when entering the TIG-30 at R3, so that caused that P21 was searching for a solution "backwards".
SPS-3 burn prediction was obtained at GET 024:13:53 and was.:
HA +0268.5
HP +0104.0
DVR +2549.6
Star check was passed at TIG-30 minutes.
Burn was performed using SPS at GET 25:14:47. Full stroking was applied at T+63 seconds. It was observed that DAP was slow to correct yaw. Pitch was coming to the center. MTVC was taken at T +3:59. Control was controllable, attitude went a little bit off right at MTVC takeover, expected and correct actions taken by crew. Burn duration was 4 minutes and 43 seconds. Both banks were used. Residuals as follows:
+00001
-00008
-00010
EMS Counter: -6.4
Not nulled as per mission rules.
Post SPS-3 orbit was:
HA +0266.7
HP +0105.8
SPS Oxid and fuel were 24.2% and no unballance after SPS-3. No ullage was used. SPS-3 was declared a good burn.

SPS-4 burn:
PAD for SPS-4 burn, wich was intended to change to a 271*115 orbit was received at GET 026:50:00. Was as follows:
MANEUVER UPDATE (P30)
SPS-4 PURPOSE
+00028 HR TIG N33
+00020 MIN
+058.08 SEC
-0001.7 DVX LOCAL VERT N81
-0299.7 DVY
-0000.0 DVZ
+0299.7 DVR N42
+0293.4 DVC
0:28.5 BT
+32591 CSM WT N47
+001.47 PTRM N48
-000.81 YTRM
23 SXTS
005.10 SFT
15.271 TRUN
-017.36 LAT NAV CHECK
+140.50 LON
+0198.6 ALT
000 R
000 P
000 Y
Remarks: None
Click to expand...
An state vector was uplinked from MCC, and P21 agreed with the NAV Check portion of the SPS-4 maneuver PAD.
SPS-4 burn prediction was obtained at GET 026:58:08 and was:
HA +0266.2
HP +0105.6
DVR +0299.7
Star check was passed at TIG-30 minutes.
Burn was performed using SPS at GET 28:20:58. Burn duration was 28 seconds. Both banks were used. Residuals as follows:
-00001
+00027
+00013
EMS Counter: -6.7
Not nulled as per mission rules.
Post SPS-4 orbit was:
HA +0264.9
HP +0105.6
SPS Oxid and fuel were 19.6% and no unballance after SPS-4. 4 jets 18 seconds ullage was used. SPS-4 was declared a good burn.

G&N power down:
At GET 028:53:35 G&N was powered down for the second night in space.
Crew started an sleep cycle between GET 030:12:00 to GET 039:02:00.
 

STS

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Flight day 3:
With a wake up at 39:02:00 and another proper but this time not very restfull sleep cycle, flight day 3 started, finally featuring the first LM activities to be performed on LM-3 "Spider" in space:
  1. Tunnel pressure verification & equalization
  2. G&N Power up (CM)
  3. Tunnel & LM hatch opening, IVT to LM
  4. LM activation (LM EPS Activation and Checkout & LM to internal power)
  5. Tunnel & LM hatch closure. (CMP stays on CM, LMP & CDR stays on LM)
  6. Continue LM activation & Daylight AOT star visibility check
  7. LM Landing gear deploy
  8. LM / CSM comm checks
  9. TV Transmission (from LM)
  10. LM G&C Systems turn on (LM PNGS turn on, AGS self check, IMU docked coarse align, LM RCS Pressurization and Cold Fire, LM Gimbal drive check, Throttle check, RCS Hot Fire
  11. DPS pressurization and DPS Docked burn
  12. LM & Tunnel hatch opening
  13. LM initial power down and final deactivation
  14. IVT to CM, LM & tunnel hatch closure
  15. SPS-5 burn
  16. G&N power down
Tunnel pressure verification & equalization:
As the first step before entering to enter the LM for the first time in space, Tunnel press was verified at GET 39:27:58, showing 1 PSI differential pressure between CM and LM.

G&N Power up (CM):
Procedures to power up the guidance system of the CM were started at 40:51:40 GET, and completed at 41:05:00 GET. CMC power up went without issue.

Tunnel & LM hatch opening, IVT to LM:
State vector and desired REFSMMAT was uplinked at GET 41:10:46. NAV check PAD agreed with state vector on AGC, by using P21. After the uplink was completed, AOT Star observation PAD was received. I´ll quote it later.
Tunnel hatch was removed at 41:58:15 GET.
LM overhead hatch was opened at 41:58:45 GET. (For NASSP team: I needed to F3 to Spider to open the overhead hatch. Can we open the LM hatch from the CM? That would be cool)
IVT to LM started at 42:00:00 GET, and initial LM inspection passed. Everything was installed and seated correctly, no debris of any kind was found.

LM activation (LM EPS Activation and Checkout & LM to internal power):
Initial activation procedures and checklists were started at 42:05:11 GET. Completed without anything special to comment, and LM was switched to internal power (CSM LM power OFF) at 42:12:50 GET.

Tunnel & LM hatch closure. (CMP stays on CM, LMP & CDR stays on LM):
Procedures and checklists continued to run without anything special to comment. LMP was switched to LM´s ECS at 42:37:40 GET. CDR was switched to LM´s ECS at 42:38:45 GET, and IVT´d to LM, and tunnel hatch was closed. LM overhead hatch was closed at 42:42:40 GET.

Continue LM activation & Daylight AOT star visibility check:
LM activation continued, crew condition was shown CRITICAL on Project Apollo MFD, for the crew that was on the LM. I experienced that on training, and considered no issue, but keeped and eye on things.
PAD for AOT daylight star visibility check was:
LM AOT STAR OBSERVATION
043 HR
055 MIN
000 SEC
2 AOT DETENT
15 NAV STAR
056 R
044 P
341 Y
CSM started an auto maneuver to the star observation attitude at 43:40:55 GET.
Explosive Devices Battery voltage was recorded as per checklist before the observation check and was as follows:
43:56:45 GET
ED A volts: 36.5V
ED B volts: 36.5V
Dimmest star seen through AOT was Procyon (15). Observation was done at 44 hours GET.

LM Landing gear deploy:
With an activated LM (but yet without the guidance part) comm modes were checked and landing gear was put down at 45:00:40 GET, with "gear down, 1 gray" indication. Deployment could be partially seen from the front windows and the CM.
Crew observed that the suit temperature increased on the LM, and that it was required to operate the valve a few clicks to the HOT position to put the temperature down.

TV Transmission (from LM):
Checklist for configuring LM communications for TV transmission started at 46:25:57 GET, and TV circuit breaker was closed at 46:27:29. And a live picture of the LM interior was shown:
1676129972200.png

Transmission concluded by pulling the TV circuit breaker at 46:34:39 GET.

LM G&C Systems turn on (LM PNGS turn on, AGS self check, IMU docked coarse align, LM RCS Pressurization and Cold Fire, LM Gimbal drive check, Throttle check, RCS Hot Fire:
Guidance systems for LM-3 were started to be turned on for the first time in space at 47:16:25 GET. LGC self check passed at 47:24:40 GET. AGS was switched to Operate at 47:26:15 GET. IMU coarse align was completed at 47:35:15 with the following gimbal angles: R: +24043 P: +24013 Y: +00030. PIPA BIAS check, at GET 47:38:00, showed all balls for 1452, 1454 and 1456 (Noun 1).
RCS pressurization started at 47:39:10. Helium pressure for RCS (Explosive devices) was fired at 47:39:36.
RCS cold fire was started at 47:42:15 GET, completed at 47:46:40, so it was determined that Spider could fly.
At 47:50:00 GET, the DAP PAD was copied:
+31953
+30678
+00642
+00695
At 48:00:00 GET, an uplink was received, containing CSM and LM state vectors.
Gimbal and throttle were tested and passed tests, starting at GET 48:02:00.
RCS hot fire was performed, also with A+ score between GET 48:06:00 and GET 48:09:30. Spider can fly!

DPS pressurization and DPS Docked burn:
At GET 48:10:00 the DPS Docked burn and a uplink was performed to the LM. Uplink contained LM state vector, a V66 and a REFSMMAT.
Pad for the LM P30 maneuver was as follows:
LM MANEUVER (P30)
DOCKED DPS PURPOSE
+00049 HR 33
+00034 MIN TIG
+04516 SEC
-0057.7 DVX 37
-1742.9 DVY LOCAL VERT
-0000.6 DVZ
+1743.9 DVR 42
000 R FDAI INER 18
000 P
-000563 DVX AGS
-1742.9 DVY
-0012.6 DVZ
Remarks: None
IMU gyro torquing angles were received at 48:15:00 GET and with those an IMU fine align was performed:
+00091
-00058
-00023
Landing and Rendezvous radar tests were performed.
At GET 48:28:54 a bump on the road was hit as the spacecraft showed a gimbal lock warning. CSM was left in FREE by mistake, and it was drifting. A quick check if the CSM attitude showed that indeed we were close to that attitude, so a maneuver from the CSM was performed to get out of there, while carefully monitoring LM´s FDAI ball. Situation was back to normal at 48:30:48.
Maneuver to AGS calibration attitude was performed by the CSM at 48:32:08 GET. AGS was initialized with a 40h BIAS, and @rcflyinghokie ´s spreadsheet was used for the time calculations to be inputted on the DEDA. After AGS/PNGS were aligned, addresses 540, 541, 542, 544, 545 and 546 were checked and showed all balls.
At GET 48:47:20, addresses 544, 545 and 546 were checked again, and were -00005, -00001 and -00009 respectively.
DPS Pressurization and checkout were performed starting at GET 49:00:37. Descent propellant isolation valve was fired at 49:01:15. He press descent start was fired at 49:01:22.
At 49:05:00 another gimbal torquing PAD was received:
-00002
-00016
-00021
CSM started an auto maneuver to the burn attitude at GET 49:10:00.
A post burn prediction was obtained on the AGC at GET 49:17:22 and was:
HA +0265.6
HP +0105.3
DVR +1743.4
LGC obtained its prediction at GET 49:21:42 GET and was the same that with the AGC.
LM performed the maneuver to burn attitude at 49:27:43 GET.
DPS engine ignited at 10% power at GET 49:34:45. Burn time vs power went as follows:
T+ 5 s: 40% manual throttle, achieved at T+ 7 seconds
T+ 26 s: FTP auto throttle, achieved at T+ 27 seconds
T+ 310s: 40% manual throttle, achieved at T+ 310 seconds
T+ 312s: 10% manual throttle, achieved at T+ 318 seconds
T+ 320s: 40% manual throttle, achieved at T+ 323 seconds
T+ 333s: 25% manual throttle, achieved at T+ 334 seconds
T+ 341s: 40% manual throttle, achieved at T+ 343 seconds
T+ 369s - Shutdown
Shutdown was commanded at -3 seconds to auto shutdown. Residuals were as follows:
LGC:
+00082
-00000
-00001
AGC:
-00084
+00042
-00043
EMS Counter: N/A

Attitude was very stable through the burn, and Gumdrop didn´t separate.

At GET 49:51:10 the following registers from the AGS were read. They showed:
544: -00005
545: -00001
546: -00009
LM & Tunnel hatch opening:
Tunnel hatch was opened from Gumdrop at 50:03:55 GET. LM overhead hatch was opened at 50:31:58 GET. CDR and LMP switched to CM´s ECS system. CDR IVT´d to CM at 50:33:00 GET.

LM initial power down and final deactivation:
Explosive Devices Battery voltage was recorded as per checklist and was as follows:
51:06:35 GET
ED A volts: 35.3V
ED B volts: 35.3V
LM was put into CSM power at 51:10:20 GET.
Procedures for the deactivation of the lunar module as completion of today´s activities were completed at 51:10:45 GET.

IVT to CM, LM & tunnel hatch closure:
LMP performed an IVT to the CM at 51:10:50 GET, and the overhead and tunnel hatches were closed at 51:11:05 GET.

SPS-5 burn:
PAD for SPS-5, that was intended to circularize the orbit for the FD5 rendezvous, was received at 52:50:00 and was:
MANEUVER UPDATE (P30)
SPS-5 PURPOSE
+00054 HR TIG N33
+00019 MIN
+036.83 SEC
-0175.3 DVX LOCAL VERT N81
-0355.6 DVY
+0425.2 DVZ
+0581.4 DVR N42
+0573.3 DVC
0:44.4 BT
+30635 CSM WT N47
+001.23 PTRM N48
-000.86 YTRM
30 SXTS
30.77 SFT
-04.859 TRUN
-000.43 LAT NAV CHECK
-137.49 LON
+0160.0 ALT
000 R
000 P
000 Y
Remarks: None
An state vector was uplinked from MCC, and P21 agreed with the NAV Check portion of the SPS-5 maneuver PAD.
SPS-5 burn prediction was obtained at GET 053:07:11 and was:
HA +0138.9
HP +0131.7
DVR +0581.4
Star check was passed at TIG-50 minutes.
Burn was performed using SPS at GET 54:19:37. Burn duration was 45 seconds. Both banks were used. Residuals as follows:
-00006
+00042
+00012
EMS Counter: -8.3
Not nulled as per mission rules.
Post SPS-5 orbit was:
HA +0136.9
HP +0132.6
SPS Oxid and fuel were 12.5% and no unballance after SPS-5. 4 jets 18 seconds ullage was used. SPS-5 was declared a good burn.

G&N power down:
At GET 055:50:10 G&N was powered down for the third night in space.

Crew started an sleep cycle between GET 058:37:00 to GET 066:41:30. First seen on this FD, it was discovered that the "stuttering issue" that I start to get while being on the CM´s VC goes away if you switch to the LM and then back to the CM.
 
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STS

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Flight day 4:
With a crew leaving the sleep station at 66:41:30 GET, the day featuring the first EVA of the Apollo program is starting. Need to test those PLSS backpacks! Activities for FD4 were as follows:
  1. Tunnel pressure verification & equalization
  2. G&N Power up (CM)
  3. Tunnel & LM hatch opening, IVT to LM
  4. LM activation
  5. Tunnel & LM hatch closure
  6. Depressurization of LM and CM and hatches opening
  7. EVA (Performed by LMP and CMP)
  8. Hatches closure and repress of LM and CM
  9. LM deactivation
  10. Tunnel & LM hatch opening, IVT to CM.
  11. G&N Power down (CM)
Tunnel pressure verification & equalization:
Tunnel pressure was verified and pressure equalization was started at 67:01:30 GET. The differential pressure was 0.3 PSI.

G&N Power up (CM):
Prodedures to bring up the CM´s guidance and navigation after the night were started at 68:00:00 GET and completed at 68:15:30 GET. CMC power up went without issue.

Tunnel & LM hatch opening, IVT to LM:
Tunnel hatch was removed at 69:00:45 GET, and LM overhead hatch was opened at 69:20:15 GET, and LMP IVT´d to LM.

LM activation:
LM activation for EVA started at 69:21:30 GET. LM was switched to internal power at 69:35:16 GET. CDR IVT´d to LM at 70:12:20 GET.

Tunnel & LM hatch closure:
LM overhead hatch was closed at 70:13:15 GET. Tunnel hatch was reinstalled at 70:13:50 GET. Tunnel was unpressurized after the closure. Unpress finished at 70:19:30 GET.

Depressurization of LM and CM and hatches opening:
After having lunch and completing some additional ECS checkouts, LM was started to be depressurized at 72:49:40 GET, completing the depress at 72:56:35. Forward hatch was opened at 72:57:05 GET, from the 2D view. I was clickling on the wrong clickspot on the VC.
CM was started to be depressurized at 72:57:56 GET, completing the depress at 73:08:55 GET. CM hatch was opened at 73:09:07 GET.

EVA (Performed by LMP and CMP):
LMP started his EVA at 73:09:31 GET.
CMP started his stand up EVA at around 73:15:00 GET.
LMP ingressed the CM at 73:28:00, completing the emergency crew transfer demo.
A TV transmission from the LM, practising for the first steps on the moon, started at 75:04:42 GET. Some audio tests from Rusty´s equipment were performed. TV transmission was completed at 75:17:04 GET.
EVA was completed at 75:24:20 GET, with an EVA duration of 2 hours, 15 minutes and 7 seconds.

Hatches closure and repress of LM and CM:
LM forward hatch was closed at 75:25:00. LM cabin repress started at 75:26:55 and completed at 75:28:07 GET.
CM side hatch was closed at 75:28:41 GET. CM repress started at 75:30:09 GET with the Repress O2 valve up to 3 PSI. Tunnel pressure equalization valve was opened at 75:31:04 GET, and it was observed that the CM cabin press was increasing again. LM overhead hatch valve was put into the open position at 75:32:12 GET, and back to AUTO at 75:33:30 GET, wrongly assuming that the tunnel was already pressurized (was still depressed):
1677415213784.png


This caused confusion on the crew as CM cabin pressure was increasing slowly, don´t understanding what was wrong (when putting the overhead hatch back to auto, the valve closed so the air flow was much reduced). Crew took a corrective action at 76:17:41 GET, of putting the overhead hatch to Open for 3 seconds, then back to Auto (tunnel was now pressurized, not knowing yet). Another corrective action was taken at 76:23:36, by setting said valve to Open, and returning it to Auto at 76:43:25.
CM repress was completed at 76:30:00 GET, so we were behind flightplan. (No much issue, just needed to do procedures faster).

Tunnel & LM hatch opening, IVT to CM:
After completing LM deactivation steps, LM overhead hatch was opened at 76:43:07 GET, CDR IVT´d to CM at 76:46:20 GET.

LM deactivation:
LM deactivation started at 76:50:00 GET. LM was put into external power at 77:53:40 GET. Deactivation was complete at completed at 77:56:00 GET.

G&N Power down (CM):
At GET 078:03:40 G&N was powered down for the fourth night in space.

Crew started an sleep cycle between GET 079:20:00 to GET 086:30:00.
 
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